Damaged Riser Causes Temporary Production Shut-In at Bualuang Oil Field

Salamander Energy announces that due to a damaged production riser, production from the Bualuang oil field has been temporarily shut-in.

During bad weather conditions, the Rubicon Vantage FPSO drifted into the exclusion zone designed to protect the production infrastructure. The Vantage’s mooring chains then came into contact with, and damaged, the production riser resulting in a small amount of oil being observed on the surface.

Production was immediately halted and operations commenced to clean up the discharge, estimated to be approximately 20 barrels. The situation was contained and all oil was successfully dispersed within a five hour period.

Further inspection work and repairs are underway. The FPSO owner has made arrangements for a new production riser to be fitted if required, which on current schedule would see production re-commence around 25th January 2014. Salamander does not anticipate that it will incur any significant repair costs.

Development drilling is not impacted by these events and the Atwood Mako rig remains on the Bravo platform and is currently drilling the BB-02H well. Salamander will use the opportunity provided by this period of downtime to accelerate planned maintenance and has rescheduled some of the hook up work on the recently installed process modules. The new FSO, that will be installed later this year, will have a turret mooring system with 360 degree swivel capability with no need for an exclusion zone and hence the risk of this kind of incident being repeated will be removed.

Despite the shut-in the Group’s production forecast for 2014 remains unchanged with production expected to average between 13,000 and 16,000 boepd.

Press Release, January 08, 2014

 

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6th Offshore Well Intervention Conference Gulf of Mexico

The Offshore Well Intervention Gulf of Mexico conference (OWI GOM) is returning to Houston, Texas for its sixth year on Wednesday 20 – Thursday 21 November.

Featuring Anadarko, BP, Shell, Chevron, BHGE and Oceaneering, the conference aims to help operators transition to the latest compliance updates, WI systems and business models that enhance safety, quicken well access and improve commerciality.

Across two days, more than 200 delegates, 15 exhibitors and 30 speakers will network together and create solutions to some of the most pertinent industry challenges right now, through a conference programme focused on:

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For registration, speaking or sponsorship enquiries contact Abigail Clifton on aclifton@offsnet.com; +44 (0) 203 793 8800.

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